2009-07-31

Big Update - Big Changes

Well, after my trip abroad I'm back and we've finally cleaned up the car. The good news is, the NUB63T is running (sort of). The bad news is that its still a bit rough.

While I was gone, Carmen did a fair amount of work. The most noticable is the new stereo, to replace the hole in the dash that was there originally.



On sale from JB HiFi.



Fitted with help from our mate Matt, who helped untangle the mess of wires in the dash.

We also picked up a set of door trims to replace the ratty ones that were there, and they came with speaker mounts (and speakers). Since the head unit came with speakers she decided to fit them instead.



Looks pretty classy.

The other major addition is new hatch dampers.



The old shocks were dead, so you had to hold it up yourself. A right pain in the arse when you're trying to load the boot. With a steel hatch, the thing weighed a ton. It could probably take someone's head off if they weren't wary.


However, the biggest job was the one we couldn't do ourselves. That is, the stupid coolant leak. The service manual makes it sound so easy, "Undo all the belts, move the engine out of the way, replace it" like its replacing the windshield wipers.

At any rate, we gave Andrew, The Engine Whisperer, a call and he came around to do it for us. He did make it look easy, but still not in a way we'd like to attempt by ourselves.

It turns out that "moving the engine" is as simple as putting a trolley jack under the sump, undoing a mount,



and then using the jack to lower the engine a bit.

To be honest, he came over twice. The first time we got to the point where we had moved the engine and pulled all the belts off. However, trying to get the crank pulley off ended up with the bolt winning.



The offending bolt.

But, with the assistance of an upgraded air compressor, and a screwdriver into the gearbox, he managed to get it off.



The claw works a lot better when you can loosen the bolt.

We were going to do the timing belt as well, but just in case Andrew locked the existing belt in place "as good practice" so we wouldn't have to set everything back up afterwards...or risk destroying the engine.



It was just as well. It turns out the timing belt we bought off eBay, that was "definitely for the GTi", was too short. It looked like it came off a SOHC vehicle, as there was no way you'd get the belt wrapped around both cam gears and the pulley. Lucky it was only $10. So, we've still got the existing timing belt, and Andrew's good practices saved us a lot of time.



The block, de-pumped.

As for the pump itself, it had clearly seen better days.





You can see the stains where it was leaking out of the pump. The water was trickling down the engine block, and following the seal around to leak at the front where we could see it.




So, with a shiny new pump in its place (this one actually fit the car) everything got put back together. And, we finally put it back on the road. Kind of.



Unfortunately the car hadn't been driven for a while, so the battery was deader than disco. We thought we'd take it out for a drive.

Unfortunately, the new intake pipe is a trifle too long for the engine bay. I don't know what Swift it came off, or if our chassis is just too bent, but it just won't fit.

The pod filter was touching the back of the headlight, and the middle of the pipe touches the strut tower. The vibration from the engine pushes the pipe against these things, and leverages open the silicon hose we use to join them.

As such, the intake bleeds air. Unfortunately, most of the air is past the airflow meter and so the car runs rich, we lose throttle, and then the car stalls. With a dead battery the car was really reluctant to start afterwards. We got lucky that, the first few times, we were downhill so we could roll start the car.

Unfortunately, near Parramatta, our luck ran out. I tried to jump start the car, but due to a misunderstanding with the colour of the terminals I got the polarity wrong and blew a main fuse instead.

A quick call to Andrew and he came around to assist. In what I am sure was a funny sight, he plugged his soldering iron into a power point at the nearest servo and soldered the fuse shut.



It would be enough to get the car running, but he warned me that if I did the same thing again I would fry something far more important.

So, lining up a new battery and a new fuse, the car was left in a "basically running" state. Enough to do the grocery shopping and for us to ferry around a friend, which is better than the other cars we own.

2009-06-27

Let the replacing begin.

So Alan left for Europe so I spent the day fixing parts on the car.
Put in a new battery tray and clamp since the battery tray was previously held in by cable ties.



Went to replace the intake pipe but after spending time cutting all the silicon piping to fit, after attaching the air filter I had a bit of a problem:



Managed to JUST fit it into the engine bay [will post up pics after] and spent time replacing the radiator:



The rear bumper is now held on by cable ties since I discovered the fight side had somehow popped out and was rsting on the rear wheel.

The "To-Do" list is slowly shrinking...

2009-06-25

Quick Update.

Well since I haven't had much time due to uni exams, the car still remains as being full of problems. We did take the car to TyrePower at Hornsby to get new front tyres [RE001s] as well as get new wheel studs. Since the wheel was off as well we decided to get Sujith to do the bearing which saves me from trying to get the calliper bolts off myself. Sadly on our way to TyrePower, we snapped the clutch cable which meant the car had to be towed to Sujiths. :(
Wasn't that surprising since it was having problems engaging gears the previous night causing us to hold up traffic while trying to push it into a parking spot.

New air filter just as a replacement while the other one is being cleaned.



Also, picked up the NUB63T plates from the RTA




Pile of stuff to go into the car:

- water pump
- radiator
- boot struts
- intake
- door trims
- Interior plastics
- spare tyre
- battery tray/clamp
- extractors
- Timing belt

2009-06-14

Fixing the Headlight.

So for the last couple of days, the left headlight has looked like this;
We stuck tape around the right headlight as well just for consistency. Basically this is what happened to the left hadlight: So I finally bothered to take out the super-glue and fix it today. This glue is $2 for a 10 pack at the reject shop and it's probably the best glue I've ever used. Works extremely quickly and is extremely strong. Will probably take off the air filter in the next few days for a clean also:

2009-06-11

Pain in the Back



So, NUB63T is a little weepy right now. The car's been shedding green tears.

We knew about the coolant leak when we bought it, but it doesn't appear to be leaking from the pump. It seems to be coming out from the bottom of the block.

It'd been leaking a crapload more fluid than we expected. It's not particularly drivable until we get this resolved. At least its stupidly cold in Sydney right now, so hopefully its not a major issue.

We're trying to see if it can be fixed simply with some silicone sealant. We've been plugging up the holes with it for the last 2 days, and running it around between the block and the sump as a second gasket.



So Carmen and I have had the car up on stands for the last few days, poking around under the bonnet. Our backs are killing us, lying down or bending over trying to reach every nook and cranny.

We've had a work light shining on the bottom, to try and dry the stuff out quicker. It looks kind of cool, actually.



We've done it a few times now, and we're hoping it'll hold. Otherwise the car might actually need to go to someone to fix. :(


UPDATE: So I went out and checked the car.



Ut oh.



I gave The Engine Whisperer a call, and hopefuly he has some ideas. Ones that don't involve a shitload of money.

First Impressions

I've always liked the Swift GTI. I'm not sure why, but even before I drove one I thought they were a pretty cool pocket rocket.

Then again, back then I had close to no idea about cars so my opinion didn't mean a great deal.

A friend of mine let me drive his just after he had full Whiteline suspension installed. I adored the steering feel and response.

I was driving a stock Pulsar SSS at the time. The car didn't feel any stronger once you got a few revs on board, despite the 50% larger engine, and in terms of handling this little shopping cart was miles ahead.



Fast forward to now. I've got a greater understanding of cars, and a general dislike of front wheel drive. My current car isn't all that shabby either.

Still, when I first drove The NUB63T, I adored it. My current car isn't light (it weighs practically twice as much as The NUB63T) and I've missed the kind of chassis response that can only come from a lack of inertia. The steering, not being power assisted, has loads of communication. The lack of torque negates my usual issues with FWD, being the torque steering the car and corrupting the steering feel.

The car has clearly had a hard life, and its still going strong regardless. The engine is a willing little thing, despite its 12 years of age and ownership by people who I am sure were not allergic to the upper third of its rev range. The chassis, dulled with age and neglect, still shows a playfulness that makes me wish I'd gotten one earlier.

I also haven't been much of a hands-on kind of guy when it comes to running the car. I've always let mechanics or mates do work on my cars, and stuck with a theoretical knowledge of how cars work. I was always more interested in driving the thing, and letting other people fix my fuck-ups.




Still, doing what little work I have done so far on the car has been surprisingly fun. The shithouse condition of the car means I've got little fear of breaking it (only breaking it more), and unlike my previous cars I didn't sink a year's income into the buying it.

This car could be, to quote Leno on the R35 GT-R, a car to build a relationship with. Which wasn't quite in the original brief, but a great thing nonetheless.

2009-06-09

Day 5.

[09/06/09]

Had to go to SuperCheap Auto today to buy a few things so I treated myself to a new toolbox and tools;



Bought a new oil filter as well as new bulbs since the bulb for the left indicator was burnt out.
Flushed out all the old horrible black oil and changed the filter.



Jacked up the car to change the wheel bearing but the caliper mount bolts were being stubborn so I decided to leave it to another day since it was getting dark and cold.

2009-06-06

The Birth of The Nubget.

[06/06/09]
Finally bought a run-around to drive since I am doing stupid amounts of mileage on the NC and the Z is having wear and tear issues. Plus I've been wanting a car I can work on myself for AGES. Bought this 1995 Swift GTi the other day mostly on impulse since the engine sounded awesome. Nice grunt from the exhaust and the engine was kept in good condition, however everything else needs some tidying up:
- no speakers/sound system,
- bonnet doesn’t sit properly,
- boot dampers don’t work,
- wrong size tyres and therefore cause scrubbing,
- missing wheel nuts,
- windows not winding up properly,
- chassis a little bent from a previous crash,
- random parts of the dash that fall off,
- battery held in by cable ties,
- random wiring hanging out,
- random screws missing here and there,
- rear wheel bearing needs replacing,
- radiator/overflow storage full of brown sludge,
- rear windscreen wipers don’t work
- the front windscreen wipers go off at random intervals

yet I have fallen completely in love with this car.











Spent the day cleaning up the easy stuff:

Random bits that I pulled out of the car [glove-box, under the seats, pockets behind seats];



Pulled the dash apart to spray the white bits and the “fully sick M3 mirrors”. Alan helped spray the parts black. Sadly, we both suck at spray-painting so it turned out very bubbly. I will find time to sand it back and re-spray it.



Flushed out the radiator and also had to clean out all the gunk in the overflow storage. For some reason, there wasn’t a way to actually take out the unit without breaking it since it seemed like it was welded/super-glued in so I spent most of the night flushing it out with this awesome contraption.



Finally got the tank white again after lots of water and stupid amounts of pumping.
Put in new coolant, topped up the oil and put all the parts I sprayed back onto the car.

Will find tie between exams to change the oil/oil filter and bearings in the next few days.